by Hudson2640
A P32 and a single car were added to the front of the train. The disconnect was between that first and second car. My money is on a defective draw bar.
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DutchRailnut wrote:the drawbar or coupler did not fail , it just uncoupled.Could have been a cracked knuckle that failed en route though. Do you have a source inside Amtrak, or are you just assuming?
DutchRailnut wrote:yes but not revealing them as it would target employee.Understood, and thanks.
Backshophoss wrote:This has got to be one of the RARE times the pin in the coupler didn't seat right/drop in place,yet it did pass the tug test.There's a joke among the model railroad community is that the train ran over a powerful magnet and the pin was pulled out right at that point, just like on Lionel train models. :D
It's Murphy's law at work!
Hudson2640 wrote:After re-reading some of the news articles, the emergency cord was pulled in the first car, AKA the car that was still attached to the ENGINE. The breaks on the 5 detached coaches worked as intended. People were probably freaking out the engineer would never notice and would bring the train all the way to Hudson before every realizing what had happened. So the whole story of the guy being a big hero is kind of BS.The news is quite muddled about where in the train the disconnection happened. Do you think the conductor was in the section that was left behind?